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JerryR
Joined: 07 Feb 2008 Posts: 167
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Oscillator issue? |
Posted: Fri Mar 08, 2024 9:15 am |
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Hello Group:
I have an issue with a target using a PIC18F1220. Using CCS IDE v5.093 with ICD-U80 debugger.
Debugger works well with one prototype target, but this particular taget will not debug. When loading code, debugger responds with "Target program not running".
I have used CCS Load to manipulate MCLR (all okay), correct voltage shows up, but oscillator fails internal 8MHz.
Guess I could have a bad PIC?
Anyone see anything wrong with the simple code attached, particularly in osc selection?
Thanks for more good eyes.
Code: |
#include <18F1220.h>
#include <ElecChoke (Rev A).h>
void Get_Pots(void);
void Set_Limits(void);
//=============================================================================
//=============================================================================
//Get all pots
void Get_Pots(void)
{
set_adc_channel(0); //get pedal input
Choke_Pos= read_adc(); // Read from AN10 and store in BS
delay_ms(1);
set_adc_channel(2); //get Low Speed input
Max_Ret_Pos= read_adc();
delay_ms(1);
set_adc_channel(3); //get Accel input
Max_Ext_Pos= read_adc();
delay_ms(1);
}
//=============================================================================
//=============================================================================
void Set_Limits(void)
{
if (Choke_Pos <= 184) //force bounds of servo
Choke_Pos = 184;
if (Choke_Pos >= 925)
Choke_Pos = 925;
}
//=============================================================================
//=============================================================================
main()
{
// Setup the ECCP for PWM in half bridge mode.
setup_ccp1(CCP_PWM);
// setup timer 2 for 25kHz
setup_timer_2(T2_DIV_BY_16, 1000, 1);
setup_adc_ports(sAN0 | sAN1 | sAN2 | sAN3, VSS_VDD);
setup_adc(ADC_CLOCK_DIV_8); // A/D clock/8 @8MHz,Tad=1uS
output_high (Servo_PWR);
while(1)
{
Get_Pots();
Set_Limits();
set_pwm1_duty(Choke_Pos);
}
}
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Code: |
#device ADC = 10
#fuses NOWDT, BROWNOUT, PUT, NOLVP
#USE delay(internal=8mhz)
#define Servo_PWR PIN_B4
int16 Max_Ext_Pos;
int16 Max_Ret_Pos;
int16 Choke_Pos;
int16 Accel;
int16 Pedal;
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Ttelmah
Joined: 11 Mar 2010 Posts: 19529
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Posted: Fri Mar 08, 2024 10:03 am |
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I the OSC2 pin is available to you, enable the clock out, and probe this
pin with an oscilloscope.
The oscillator can be unreliable if the supply is not well decoupled, but
I must admit the most likely cause is the chip itself. |
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JerryR
Joined: 07 Feb 2008 Posts: 167
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Posted: Fri Mar 08, 2024 10:27 am |
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Yes, I'll try to see if anything appears on OSC2, good suggestion.
Power supply should be well decoupled with 0.1uF and 10uF at the PICs pin.
Thanks! |
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